| Project: | Keller Trust #1 West |
|
|---|---|---|
| October 2010 |
| Day | Date | Operation | ||
| Pre-Drill | Sunday, October 17 | Begin preparing location, start digging pits. | ||
| Monday, October 18 | Begin moving rig components to loc. | |||
| Tuesday, October 19 | Rig up and begin moving water to pits. Take delivery of surface casing. | |||
| 1 | Wednesday, October 20 | 6:30 am Begin drilling surface hole. | ||
| 2 | Thursday, October 21 | 7:00 AM Drlg. at 775 ft. Cemented 89 ft. 8 5/8th surface casing. Used 100 sacks. Plug down at 2:00 PM. Resume drilling at 8:30 PM Straight hole test at 500 ft. = o degrees. |
||
| 3 | Friday, October 22 | 7:00 AM Drilling at 1750 ft. Straight hole test 1000 ft. = 3/4 degree 1500 ft. = 1 degree |
||
| 4 | Saturday, October 23 | 7:00 AM Drilling @ 2487 ft. Roseclair, wet 1:00 PM McCloskey @ 2542 - 2550 , Oolitic lime, strong odor, good show of oil. |
||
| 5 | Sunday, October 24 | 7:00 AM Drilling at 2817 ft. Straight hole test; 2500 ft. = 3/4 degree |
||
| 6 | Monday, October 25 | Total depth 3000 ft. Weatherford International logs well. Run 4 1/2" production casing to 2600 ft. (McCloskey). |
||
| 7 | Tuesday, October 26 | 7:00 AM Ran 2600 ft. of 4 1/2'" production casing. Schwartz on loc. to cement with 365 sacks. Plug down at 4:45 PM. |
||
| Project: | Martin Trust #1 |
|
|---|---|---|
| September 2010 |
| Day | Date | Operation | ||
| Pre-Drill | Thursday, September 16 | Begin making loc. with cat and backhoe. | ||
| Friday, September 17 | Move Deep Rock Drlg. Rig to Loc. Dig pits. | |||
| Monday, September 20 | Move water to 500 bbl. frac tank and fill pits. | |||
| 1 | Tuesday, September 21 | Spud well. Set 81 ft. 8 5/8 surface casing. Schwartz cement with 75 sx. Plug down at 2:30 PM. Shut down for cement to set. |
||
| 2 | Wednesday, September 22 | Begin drilling at 2:30 AM. 7:00 AM Drlg. at 800 ft. Straight hole test at 550 ft. = 1 degree. |
||
| 3 | Thursday, September 23 | 7:00 am Drlg @ 1790 ft. Straight hole test at 1090 ft. 1 degree,1500 ft 3/4 degrees |
||
| 4 | Friday, September 24 | 5:00 am, Benoist SS at 2290 ft. Drilled 8 ft. and stopped to condition hole for DST and trip out of hole. Cuttings had good odor, good florescence, porosity and a cut of live oil. 9:00 am Start tripping into hole with test tool. |
||
| 5 | Saturday, September 25 | 10:30 am Friday DST tool misfired due to 15 ft. of fill up in bottom of hole.
Trip out of hole, clean tool, trip into hole to recondition mud and bring viscosity to 85. Circulate for 2 hours. Trip out of hole. Trip back in with test tools. 10:00 pm Friday Begin DST on Benoist. 12:10 am Sat. End test and trip out of hole. DST results; 210 ft. drilling mud, show of live oil in tool, end 1 hr. test 850 psig. Bottom of tool had shale chips blocking some perfs. 7:00 am Resume drilling. Aux Vases at 2342. drilled 12 ft. Good odor, good flouresence. Straight hole test at 2000 ft. = 3/4 degree. |
||
| 6 | Sunday, September 26 | 7:00 am Drlg at 2704 ft. (St. Louis Lm).
Call depth at 2860 ft. (Salem Lm) Straight hole test at 2542 ft. = 1/2 degree |
||
| 7 | Monday, September 27 | 10:00 am Weatherford Well Services logging well. TD at 2965 ft.
Gas shows in Salem, no show oil. All zones calculate wet or marginal at best. Decision made to plug well. Plugging in process. |
||
| 8 | Tuesday, September 28 | 7:00 am Well plugged with 125 sacks.
Webster rig down and move off location. |
||
| Project: | Tonn Trust #1 |
|
|---|---|---|
| October 2010 |
| Day | Date | Operation | ||
| Pre-Drill | Friday, October 8 | Begin moving topsoil. | ||
| Sunday, October 10 | Begin digging pits and move rig on to location. | |||
| 1 | Monday, October 11 | 7:00 AM Rig up, finish digging pits, move water to location. Bradford delivers 80' of 8 5/8ths casing. Begin drilling surface hole. |
||
| 2 | Tuesday, October 12 | 7:00 AM Drilling at 690 ft. Cemented 81 ft. of 8 5/8ths casing with 120 sacks. Plug down at 4:15 PM. Resume drilling at 10:00 PM. Straight hole test at 500 ft. = 1 degree |
||
| 3 | Wednesday, October 13 | 7:00 AM Drilling at 1625 ft. Straight hole test; 1000 ft. = 3/4 degree 1500 ft. = 3/4 degree |
||
| 4 | Thursday, October 14 | 7:00 AM Drilling at 2152 ft. Straight hole test; 2000 ft = 3/4 degree Call depth at 2250. Benoist at 2285 ft. |
||
| 5 | Friday, October 15 | 7:30 AM DST #1 in progress. Tool on bottom at 7:10 AM Weak blow in bucket. Begin 3 hour test. Test interval 2278 - 2304 Benoist sands. Current TD at 2420 ft. Top of St. Gen @ 2411 Ft. |
||
| 6 | Saturday, October 16 | 7:00 AM Drlg @ 2710 ft.Completed DST #1 and resumed drilling at 3:40 PM, Fri. Benoist had 860 lbs. final shut in pressure. McCloskey, Good show of oil, strong odor, good fluorescence. Upper Salem, 2676-2678 VSSO, weak odor, slight fluorescence. Next call depth @ 2710. |
||
| 7 | Sunday, October 17 | 8:30 AM Weatherford on location to log well. 3:00 AM TD at 2950 ft, trip hole for logs. Show of oil in Salem at 2881 - 2887, strong odor, fair fluorescence. |
||
| 8 | Monday, October 18 | Review of logs determined well not capable of producing commercial quantities of oil. Well was plugged from 300 ft. out, according to inspectors instructions, at 4:15 PM. Rigging down and preparing to move rig to Keller Trust #1 West. |
||